Re: 4R70W 3-4 4-3 shift concern
Posted to Transmission Forum on 12/27/2017
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Resolved! I just want to close this thread out on a positive
note. The 3-4 shift problem has been FIXED. As some of you
suspected, myself included, the source of the trouble was in
the valve body, specifically, the 3-4 and Low Servo Capacity
Modulator Valve circuits. I inadvertently swapped the
springs between these two valves (thanks JK080 for the
spring arrangement info) during the initial rebuild process.
Having the lighter tension "white" spring behind the 3-4
modulator valve apparently created an imbalance in the 3-4
shift circuit. It should have had the "yellow" heavier
tension spring installed with it and the white spring
installed with the low servo valve. Now, although I did
replace the tcc solenoid and the harness assembly with new
ones this time around, I did so purely to extend the
operational life of the transmission. There were no problems
detected with either of these original components. The trans
shifts beautifully and is silky smooth at the top end with
OD, and perfect closed throttle coasting conditions without
going into that rapid 4-3 shift cycle. Thanks to all those
who offered their experience to get this one resolved!
Lance Bowling Technician/Owner Lance Auto Diagnotics Gallatin, Tennessee, USA
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